炼钢 ›› 2026, Vol. 42 ›› Issue (2): 39-45.

• 凝固与浇铸 • 上一篇    下一篇

双流中间包单流改造的流场优化和夹杂物去除效果

唐爱华,王多刚,江中块   

  1. 上海梅山钢铁股份有限公司,南京 210039
  • 出版日期:2026-04-05 发布日期:2026-03-27

Flow field optimization and inclusion removal effect in the conversion of a double-strand tundish to the single

  • Online:2026-04-05 Published:2026-03-27

摘要: 为了降低高品质低碳钢铸轧界面能耗,上海梅山钢铁股份有限公司2号连铸机实施了双流中间包单流改造,将连铸机拉速由1.2 m/min提升为2.4 m/min,进行单流高拉速的生产。针对改造后中包流场和夹杂物去除效率等问题,通过物理和数值模拟相结合的方法,研究了不同工况下中间包内钢水的流动行为和夹杂物运动轨迹。研究结果表明:单流改造后,原双流中间包的控流装置不再适合单流浇铸,其堵流侧死区较大,包内混匀性差。使用新型的湍流控制器和挡墙后,堵流侧流动情况得到改善,包内死区体积下降12.2%,响应时间延长了96.7%,平均停留时间增加了11.2%,峰值浓度降低了45.3%,表明优化后的中间包具有更好的流场。另外,优化后的中包夹杂物的去除率相比原来均有明显的提升。大样电解结果表明,优化前夹杂物平均含量较高,达到了0.78 mg/kg,优化后显著降低至0.29 mg/kg。该研究通过在中间包内引入新型控流装置组合,有效改善了包内流场,提升了夹杂物的去除效率和钢水洁净度,使得连铸机拉速显著提升,助力炼钢节能减碳。

关键词: 双流中间包, 单流浇铸, 夹杂物, 流场, 大样电解

Abstract: In order to reduce the interface energy consumption during the casting-rolling process of high-quality low-carbon steel, the No.2 continuous casting machine at Meishan Steel implemented a transformation from a two-strand to a single-strand tundish. This modification increased the casting speed from 1.2 m/min to 2.4 m/min, enabling single-strand high-speed casting production. A combined approach of physical and numerical simulations was employed to investigate the flow characteristics and inclusion trajectories under different operating conditions. The results demonstrated that the original flow control devices of the tundish were no longer suitable for single-strand casting after modification, leading to significant dead zones (particularly on the blocked-strand side) and poor mixing homogeneity. By introducing a novel turbulence inhibitor and redesigned dam, the flow pattern on the blocked-strand side was notably improved. The dead zone volume decreased by 12.2%, the response time extended by 96.7%, the average residence time increased by 11.2%, and the peak concentration decreased by 45.3%, indicating superior flow field uniformity in the optimized tundish. The removal efficiency of inclusions was significantly enhanced in the modified tundish. The results of large sample electrolysis revealed that the average inclusion content decreased from 0.78 mg/kg (original configuration) to 0.29 mg/kg (optimized configuration). The implementation of new flow control devices effectively improved flow patterns in the tundish, enhanced the removal efficiency of inclusions and the cleanliness of molten steel, significantly increased the casting speed of the continuous casting machine, and assisted in energy-saving and carbon reduction in steelmaking.

Key words: two-strand tundish, single-strand casting, inclusions, flow field, large sample electrolysis