炼钢

• 辅助技术、材料及设备 •    下一篇

武钢大型转炉顶底复吹控制实践

  

  1. (武汉钢铁集团公司 炼钢总厂三炼钢厂,湖北 武汉 430080)
  • 接受日期:1900-01-01

Practice of combined blowing of large converter in WISCO

  • Accepted:1900-01-01

摘要: 武钢三炼钢厂对转炉氧枪喷头参数及底吹流量进行了优化,转炉吹炼过程中喷溅发生频率由3.4%降低到1.5%,吹炼终点炉渣T.Fe质量分数由15.99%降低到15.49%,达到了较好的吹炼效果。通过激光测厚监视炉底厚度,延长可见透气砖寿命达4 000炉,提高底吹气体流量至1 100m3/h,在8~16个可见透气砖条件下,转炉的碳氧积在0.001 5~0.001 8,达到了较好的冶金效果。四炼钢厂优化了氧枪喷头参数及过程操作枪位,解决了废钢熔化问题。通过大气量后搅试验,优化了后搅模式,在4个可见透气砖条件下,后搅流量为500m3/h,后搅时间为3~4min,平均每分钟降低钢水氧质量分数20.47×10-6,降低碳质量分数29.23×10-6。

关键词: 喷头参数, 底吹, 透气砖, 碳氧积

Abstract: The parameters of converter oxygen lance nozzle and the bottom blowing flow rate were optimized in No.3 Steelmaking Plant of WISCO. The splashing frequency decreased from 3.4% to 1.5% in blowing process, the slag T.Fe mass fraction reduced from 15.99% to 15.49% at the end point of blowing, good blowing effect was achieved. At the condition of monitoring the bottom thickness by laser measuring thickness, extending visible porous brick life up to 4 000, improving the bottom blowing gas flow to 1 100m3/h, using 8~16 visible porous bricks, [%C]•[%O] was in 0.001 5~0.001 8 at blowing end, which achieved better metallurgical effects. The parameters of oxygen lance nozzle and the lance profile in blowing process were optimized in No.4 Steelmaking Plant, the problem of scrap melting was solved. The stirring mode was optimized through the large gas flow stirring test at the end blowing. When using 4 visible porous bricks and stirring flow 500m3/h, stirring time for 3~4 minutes, the mass fraction of oxygen reduced 20.47×10-6 average per minute in molten steel, the mass fraction of carbon reduced 29.23×10-6 average per minute.

Key words: oxygen lance nozzle, bottom blowing, porous brick, carbon-oxygen equilibrium