炼钢 ›› 2017, Vol. 33 ›› Issue (2): 57-62.

• 产品工艺与质量控制 • 上一篇    下一篇

X52抗硫管线钢冶炼工艺优化

  

  1. (1.达力普石油专用管有限公司,河北 沧州 061000;
    2.河北省石油专用管工程技术研究中心,河北 沧州 061000)
  • 接受日期:1900-01-01 出版日期:2017-04-05

Process optimization of X52 sour service pipeline steel

  • Accepted:1900-01-01 Online:2017-04-05

摘要: 抗硫管线钢生产过程中存在碳、硫、磷元素控制困难,钢铁料消耗高等问题,结合生产数据和热力学计算对其原因进行了分析,并从电弧炉熔炼、合金化、电弧炉出钢预精炼、LF精炼渣系和渣料加入制度等方面提出了改善措施。采用优化的工艺后,电弧炉出钢过程增磷质量分数从32.3×10-6降低至6.6×10-6;增碳质量分数从0.038 %降低至0.011 %;脱硫率从27.0 %提高到44.1 %,LF精炼过程的脱硫率从84.1 %提高到89.5 %;钢铁料消耗从1 130 kg/t降为1 070 kg/t,石灰消耗从85.4 kg/t降为33.1 kg/t,铝锭消耗从2.6 kg/t降为2.1 kg/t,氧气消耗从35.1 m3/t降为24.4 m3/t,电耗从445.8 kWh/t降为422.1 kWh/t,生产成本显著降低;LF精炼出站钢液的洁净度明显提高,显微夹杂物面积比降低了29.3 %。

关键词: 抗硫管线钢, 冶炼工艺, 精炼渣, 钢铁料消耗, 夹杂物

Abstract: There are some issues in the production of sour service pipeline steel, which includes being hard to control carbon, sulfur, phosphorous; high ferrous charge consumption. The root cause was analyzed by thermodynamic calculation combined with production data. The countermeasure was put forward from EAF melting, alloying mechanism, prerefining at EAF tapping, LF refining slag and raw material addition mechanism. After the optimized process was applied, at EAF tapping rephosphorization fraction decreased from 32.3×10-6 to 6.6×10-6,carburization fraction decreased from 0.038 % to 0.011 %,desulphurization ratio increased from 27.0 % to 44.1 %; desulphurization ratio in the LF process increased from 84.1 % to 89.5 %, ferrous charge consumption decreased from 1 130 kg/t to 1 070 kg/t, lime consumption decreased from 85.4 kg/t to 33.1 kg/t, aluminum consumption decreased from 2.6 kg/t to 2.1 kg/t, oxygen consumption decreased from 35.1 m3/t to 24.4 m3/t, electricity consumption decreased from 445.8 kWh/t to 422.1 kWh/t, and hence the production cost decreased significantly; the cleanness of liquid steel improved dramatically at LF end, the area ratio of micro inclusion decreased by 29.3 %.

Key words: sour service pipeline steel, steelmaking process, refining slag, ferrous charge consumption, inclusion