炼钢

• 辅助技术、材料及设备 •    下一篇

复吹转炉熔池搅拌技术及应用

  

  1. (1.东北大学 钢铁冶金系,辽宁 沈阳 110004; 2.福建三钢(集团)有限责任公司,福建 三明 365000)
  • 接受日期:1900-01-01 出版日期:2016-10-05

Technology of bath stirring in top and bottom combination blown converters and its application

  • Accepted:1900-01-01 Online:2016-10-05

摘要: 为了提高复吹转炉熔池的搅拌效果,在实验室研究了复吹转炉不同底枪支数和布置对转炉熔池混匀时间的影响。试验研究表明,底枪适合于布置在(0.40~0.65)D(D为熔池直径)的范围,底枪过多且对称分散均匀布置在同一圆周,不利于转炉整个熔池的混匀,而采用非对称相对集中的底枪布置,可以使熔池产生水平搅拌趋势,有利于整个转炉熔池混匀,缩短熔池混匀时间30%左右。在福建三钢(集团)有限责任公司实际复吹转炉应用非对称相对集中的底枪布置,可以改善转炉吹炼终点的冶金效果,1号、2号100 t转炉吹炼终点平均[%C]•[%O]由原来的0.003 1、0.003 3分别降低到0.002 6、0.002 7,1号转炉平均残锰质量分数由原来的0.183 %提高到0.212 %,终点平均磷质量分数由原来的0.016 7 %降低到0.014 8 %,平均终渣w(T.Fe)由原来的15.23 %降低到13.36 %,120 t转炉吹炼终点平均[%C]•[%O]为0.002 5。

关键词: 复吹转炉, 底枪布置, 对称分散布置, 非对称相对集中布置, 熔池混匀时间, 冶金效果

Abstract: Influence of different bottom tuyere number and configuration in top and bottom combination blown converters on bath mixing time was investigated in laboratory for improvement of BOF’s bath stirring effect. It is found from the investigation that the suitable arrange where the bottom tuyeres should be set is (0.40—0.65)D (D is bath diameter). Too many bottom tuyere number and symmetrical, dispersive and uniform configuration along the same circumference is detrimental for the whole bath mixing, while unsymmetrical and relatively concentrative bottom tuyere configuration can form the trend of horizontal mixing in the bath, which is benefit to the whole bath mixing and can decrease the mixing time by about 30%. It is proved from the application of the unsymmetrical and relatively concentrative bottom tuyere configuration in industrial converters of Sansteel, Fujian that the metallurgical results at converter blowing end can be improved. Mean product of [C] and [O] concentrations, [%C]•[%O], at end-point of blowing in No.1 and No.2 100 t BOFs were reduced from 0.003 1、0.003 3 to 0.002 6、0.002 7, respectively. In No.1 BOF, average [Mn] mass fraction at end point was increased from 0.183% to 0.212%, mean [P] mass fraction at blowing end was decreased from 0.016 7% to 0.014 8%, and average w(T.Fe) in slag at end-point of blowing was reduced from 15.23% to 13.36%. Mean [%C]•[%O] at end-point of blowing in 120 t BOF was 0.002 5.

Key words: top and bottom combination blown converter, bottom tuyere configuration, symmetrical and dispersive configuration, unsymmetrical and relatively concentrative configuration, bath mixing time, metallurgical result