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炉渣脱氧改质工艺对铝镇静硅钢总氧含量的影响

  

  1. (江苏省(沙钢)钢铁研究院,江苏 张家港 215625)
  • 接受日期:1900-01-01 出版日期:2016-04-05

Effect of slag deoxidation modification process optimization on the total oxygen content of aluminium deoxidization silicon steel

  • Accepted:1900-01-01 Online:2016-04-05

摘要: 针对铝镇静无取向硅钢冶炼过程中钢水、炉渣氧势过高,导致RH终点钢水总氧含量控制不稳定的问题,进行了转炉出钢、RH过程脱氧造渣工艺优化研究。结果表明:RH进站钢水w(O)由原工艺的(400~900)×10-6稳定在650×10-6以下,RH脱碳结束钢水w(O)控制在450×10-6以下;RH进站炉渣w(T.Fe)由原工艺的10 %~25 %降至15 %以下,RH出站渣中w(T.Fe)由2 %~12 %降至3 %以下,RH处理过程炉渣碱度均控制在3.0以上;RH终点w(T.O)由原工艺的(15~30)×10-6降至15×10-6以下,钢水洁净度较原工艺显著改善。

关键词: 铝镇静硅钢, 全氧含量, 炉渣改质, 二次氧化

Abstract: To the question of the unsteadiness of the steel oxygen content at the end of RH vacuum treatment for the aluminium deoxidization nonoriented silicon steel refining, the oxygen potential of molten steel and slag was optimized during tapping and deoxidation alloying process. Results show that the oxygen mass fraction of nonoriented silicon steel is stably controlled below 650×10-6 as it was (400-900)×10-6 before optimization. Furthermore, T.O mass fraction is controlled below 450×10-6 at the end of decarbonization in RH. With the optimization process, the mass fraction of T.Fe in slag is decreased from 10 %-25 % to less than 15 % at the beginning of RH, which is also decreased from 2 %-12 % to below 3 % at the end of RH, and the slag basicity is controlled above 3.0 during RH treatment process. T.O mass fraction at the end of RH is reduced from (15-30)×10-6 to below 15×10-6 using the optimization process, which indicated that the cleanliness of molten is significantly improved.

Key words: Al deoxidization silicon steel, total oxygen, ladle slag modification, secondary oxidation