炼钢 ›› 2015, Vol. 31 ›› Issue (1): 17-21.

• 生产实践 • 上一篇    下一篇

120 t转炉冶炼低磷钢深脱磷技术研究

吴明   

  1. 马钢第一钢轧总厂技术质量部
  • 收稿日期:2014-04-29 修回日期:2014-06-17 接受日期:1900-01-01 出版日期:2015-02-05 发布日期:2015-02-13
  • 通讯作者: 吴明 E-mail:wuming1964@sohu.com

Study on dephosphorization technology of low phosphorous steel smelting in 120 t BOF

  • Received:2014-04-29 Revised:2014-06-17 Accepted:1900-01-01 Online:2015-02-05 Published:2015-02-13

摘要: 为了达到低磷钢对成品磷质量分数小于0.010 %的要求,根据温度、炉渣碱度、渣中w(FeO) 以及搅拌等对脱磷的影响,马鞍山钢铁股份有限公司120 t转炉应用烟气分析动态控制炼钢技术,采用留渣双渣操作法,制定合理的装入、造渣、供氧制度,优化脱磷参数,通过500多炉次实践对比分析,确定合适的倒炉温度为1 540~1 580 ℃,w(C)=0.10 %~0.25 %,终渣碱度3.0~3.5,w(FeO)=15 %~23 %,及适合的搅拌强度以达到脱磷率95.2 %良好效果,实现了转炉出钢磷质量分数小于0.007 %,以及终点碳温双命中96.4 %的目标。

关键词: 转炉, 低磷钢, 烟气分析, 脱磷控制

Abstract: In order to make the requirement of phosphorus mass fraction is less than 0.010 % for low phosphorous steel, and according to the effect of temperature, slag basicity,w(FeO) of slag and mixing parameters on dephosphorization, the offgas analysis dynamic control steelmaking model was applied on 120 t BOF of Ma’anshan Iron & Steel Company Limited. “Slag-Remaining+Double-Slag” technology, suitable loading system, slagging system and oxygen supply system, optimizing dephosphorization parameter were used in steelmaking. Through the analysis and comparison of 500 experiments, dephosphorization rate 95.2 % can be achieved by taking measures such as the temperature and the carbon mass fraction of the first turning down 1 540~1 580 ℃ and 0.10 %~0.25 %, final slag basicity 3.0~3.5, w(FeO) =15 %~23 %, and suitable stirring intensity. And the phosphorus mass fraction of converter tapping is less than 0.070 % and the hit rates of carbon content and temperature both meet the requirement of 96.4 %.

Key words: converter, ultra-low phosphorous steel, the offgas analysis, dephosphorization technoiogy