炼钢

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连铸机扇形段轴承失效分析及改进措施

  

  1. 1.武汉科技大学 材料与冶金学院,湖北 武汉 430081;2.武汉钢铁股份有限公司 炼钢总厂,湖北 武汉 430083
  • 接受日期:1900-01-01 出版日期:2014-06-05

Analysis and countermeasures on bearing failure of continuous caster segment

  • Accepted:1900-01-01 Online:2014-06-05

摘要: 为提高武钢板坯连铸机扇形段轴承使用寿命,减少因轴承破损导致的异物压入缺陷,系统分析了扇形段轴承失效的原因,对扇形段设计和工艺参数的选择等方面进行了研究。结果表明扇形段轴承失效的主要原因是异常过载,提出了调整轻压下参数、优化尾坯输出模式、启动软夹紧功能等改进措施。连铸机扇形段工艺优化后,轴承破损引起的扇形段失效比例由89.7 %降低到62.5 %,扇形段平均使用周期由122天提高至140天,因异物压入导致的热轧卷板缺陷基本消除。

关键词: 连铸, 扇形段, 轴承, 失效

Abstract: To improve the service life of segment bearing of WISCO’s slab continuous caster and decrease the accident of foreign body rolled defect in slab by bearing damage, the reasons of the bearing failure were comprehensively analyzed, and the design and the process parameter optimization of the segments were studied. The results showed that the main reason for the bearing failure of the segments is abnormal overload. Then the improvement measures, such as adjusting soft reduction parameters, optimizing end slab output mode and using soft clamping function, were proposed. After caster segments process optimized, the ratio of segments failure caused by the bearing damage was decreased from 89.7% to 62.5%, the average life cycle of segments was increased from 122 days to 140 days, and the foreign body rolled defect in hot rolled coil was basically eliminated.

Key words: continuous casting, segment, bearing; failure